2000


This page is intended
as a historical/hysterical record of the the past breakages/new
breakages and soon to be breakages....and other bits that have
happened to Cartman since we first adopted him. This record is in
the order of most recent happenings at the top to the past at the
bottom.
December
2000 (72355 miles)
- New forward
facing/removable rear seat fitted. Now room for three!!
- Rear prop
removed. Diff end UJ totally shot and strip-down reveals
that no lubrication had been present on two of the lobes
for some considerable time due to the blockage of the
grease passage. A usual problem with very little past
maintenance (Photo). Both UJ's
removed and replaced with new. No-longer any snatch on
transmission pick-up or 'clutch' judder at very low
speeds. Also noticed that transfer box end of the front
prop has a slightly bad UJ. Look at replacing that also.
- Slighty
vibration (something out of balance?) and knock from the
drivetrain when the clutch is depressed at low speeds.
Probably the rear prop universal joints? Need to take a
look this week. Cheap repair if it is, approx. £15.
- Water around
my local area of Southern Hampshire is still causing
chaos on the roads and 'lanes. Believe
me..these were roads!!!!. Not
much of a problem for Cartman though! Just have to take
it easy at avoid water on the electrics and in the air
intake.

- Checked all
fluids after Bordon and the wading due to all the local
flooding. No evidence of any water ingress anywhere, even
from the slightly leaky off-side hub ball joint. Cannot
be anywhere near as bad as I thought ?
- Paint coming
off the front wing and passenger door hinges after a
heavy attack with a jet washer. All of the paint comes
from areas that I had either applied new paint over
rubbed back existing paintwork, or zinc primed bare
metal. My fault? Re-apply during the spring/summer.
November
2000 (72100 miles)
- 26th November
HBRO Off-Road driving
day at Bordon Camp. Cartman is running well and the
'novelty' of a smooth and non-jumpin' out gbx was well
worth the cost. The best days mud play that I have ever
had. Cartman is now decidedly mud splattered from the
roof down. Didn't get stuck anywhere,though it took 2-3
attempts at some points that were well dug-up late in the
day. But that's the price for having mild 'Wrangler' AT's
I suppose? Fuel consumption seems to have improved at
around 22-23 mpg but I will need to check my calcs before
I can be definite.

Now
that's a serious peace of kit !!?
- Mark at
West's when trying to check the timing had pointed out
that the distributor shaft was worn and it would be
better if this was changed. Fitted a new Lucas
distributor and a new coil at the same time. Cost for
both and delivery was £44 from MVS on next day
delivery. The advance pipe to the distributor was sucking
in air in several places so this was also repaired. The
engine no-longer wants to run on when the ignition is
shut off so that must be a good thing.
- In an attempt
to reduce the 'rattle' on the top end of the engine I
carried out an investigation into the source. With the
engine running and the rocker cover removed I could see
that the oil flow on the rear four valve rockers was only
dripping while the front four had a good rate of constant
flow. On strip-down there was a slight warp in the rocker
shaft (1.5mm) and noticable wear on the shaft the
securing pin locating the shaft in position had
broken-the oil passage holes had then moved out of
alignment. The rockers, valve rods seemed to be fine so a
new shaft was fitted and valve clearances adjusted. Oil
flow is now fine and the top end noise is far less than
before. Any noise left is due to tappet and roller
follower wear and the cam lobes. Though noise though
reduced increases in intensity after periods of low
stress such as pootling around town, if I take it for a
good run then the noise is reduced. i.e. oil pressure and
oil viscosity at high temperatures? Currently used 10/40
GTX so a trial at the next change with good 20/50 may be
in order?

Old
one out and new one in
Spot
the missing O/D teeth?
October
2000 (71600 miles)
- Sodbury
sortout was a complete washout. Should have taken some
pics for the site but the weather was so bad I even gave
that idea up for the risk of damaging the digi cam. Did
aquire both a new front recoil seat belt (if I can mod it
to fit) and a pair of new wiper arms.
- Oh nooo, have
to bite the bullet now. Gearbox has managed to generate
an additional rattle. Took it for a quick check by West 4x4 in Bishops
Waltham. Mark is insistent that it is not the detent
springs that are allowing the box to jump out of 1st and
2nd and that the noise is a symptom of both a damaged
gear in the main box (found teeth in '99) and damaged
teeth on the overdrive sliding gear assy (that's why its
so noisey?). The springs found in '99 when draining the
main box are from the synchro assy on 3rd and 4th. I
found two then so its surprising it still works? It is
now booked in for an expensive gbx drop and repair in
early November. At the end of it I should have a nice
'quiet' box and a working overdrive which will be a
novelty. So watch this space.
- Modified the
air demister blower to direct more air onto the drivers
screen than the LH passenger side. To restrict the air
flow a night light candle base with a 10mm hole through
the centre was fitted into the air duct (the night light
fitted spot-on that's why I used it). I'll see if this
improves the de-mist 'performance'.

- Bare wire
found under the front of Cartman when I was fitting the
new oil filter (surprising what you notice when you're
rolling around underneath a vehicle). The cable had been
stripped of its insulation for 3 inches. Investigation
then showed this cable to be for the rear reversing
light. Stupid place to run a cable anyway. New cable
routed inside the vehicle.
- New brake
piston fitted to the top RH front drum. This seemed to
have been dragging when Cartman had not been used for a
few days. Brakes bled through. Drivers side front hub
seal replaced & bearings re-packed.
- Engine oil
flushed and drained. New filter fitted. 750ml Slick 50
added with Castrol GTX 10/40. There is a lot of debate
whether Slick 50 gives much of benefit and whether it can
cause problems with oil way blockages, but I have used it
on all my vehicles for the past 15 years without any
problems (or proven benefits?). The LR engine being very
basic and 'agricultural' should benefit more than higher
tech motors anyway - at least that's my theory. I noticed
that the paperwork provided with the additive does not
make anywhere near as many claims to its benefits as it
did 5-10 years ago. That is probably due to the law suits
against Pennzoil in the U.S.A. some time ago against
their unsubstantiatable claims.
- Shire LRC
driving day at Brick Kiln Farm saw Cartman get stuck
between two trees and extreme mud (those that know the
site know how bad it can get. Alistair the ROW officer of
Shire LRC suffered slight embarrasment at his predicament
in 'The hole'. The only solution was to for him to be
'tugged off' the hump that he straddled his Range Rover
with.

Stuck!
-
Alistair suffers a slight altercation with a muddy mound.- Un-stuck!
After
leaving site another poor soul managed to flip his Rangey
onto its roof - and he still drove home (wheels pointing down
of course).
Whoops
- wrong way up? (Courtesy Shire LRC Web site)
September
2000 (71236 miles)
- In
preparation for the coming 'Winter' months (won't be long
now!) I have modified the washer pipework for the front
screen. After a suggestion in LRO (something useful in
LROI??!!!!) I re-ran the washer bottle pipework and
wrapped it several times around the heater matrix
pipework. My logic is if it is cold enough to require
heated water for the screen,then I will have the heater
on in the cab. Installation is as shown below. The
pipework will be wrapped in aluminium tape in the next
week.

- Green lane day with Shire LRC was
eventful with one vehicle rammed twice by a farm hand in
a tractor. His defence was ,'They were on my bosses
land'. Police called and the man questioned and cautioned
for criminal damage. The 'land' in question was a R.o.W.
listed on Hants CC definitive map (highway). Several
other club vehicles arrived and witnessed the incident.
Damage to the 'R' reg (1998) County SWB Defender will be
expensive and the shock to the lady driving it cannot be
repaid. Watch this space for a successful prosecution.
Accidental damage will not wash,as he reversed for
another go.
Update
on the above...- The Police do not
seem to be interested in a prosecution and the insurance
companies for both parties are sorting out the claim.
However, the injured party is considering a civil
prosecution. We wait to see the result?
- 1 tonne
shackles fitted. Not as straight-forward as I first
thought. A lot of precarious balancing on jacks etc. But
they are now on and the LR is looking level. Better still
the ride at the rear has improved. Don't know why but
even Liz's independent opinion agrees. See shackle info
site for details.
- Night laning locally caused a
fright. Parked on the downs, lights off at 9PM in the
blackness. Gunshot 30-50yds to my right in the brush
(.22LR probably). Didn't stop to find out who, let them
know I was there by switching on the lights and getting
the hell out of there.
- Pintle and
ball hitch aquired from the Shire LRC rally for the
pricely sum of £10 (Good man Stewart!). New price £45.
Now fitted to the Dixon-Bate hitch.
- Simple light guards made up for the
rear lights and the reversing lamp. The guard over the
reversing lamp prevents the spare tyre mounted on the
door from resting on the lens when the door is held open.
Manufactured from bent 8mm steel rod with washers mounted
at either end. Chance of accidental damage is reduced and
they are all easily removable if I have to change the
bulbs.
Guards
fitted
- Rear brake
that was reported on the MOT was resolved. The 'sticky'
rear brake cylinder was actually a return spring that had
fallen off and was resting in the assembly. So that was a
straight forward job to resolve. The flexi hose was
replaced and the system bled through. Once after the hose
was fitted and again 12 hours later just to make sure. As
I expected the worst I had already purchased another set
of SWB front cylinders - now spare - at the moment.
August
2000 (71000 miles)
- STOP
PRESS!!!!!!!!!! Fuel consumption on Cartman has
improved!!!! We are now up to 19.5MPG! Error in
calculation with tyre sizes brought this about plus the
7% CO prob. Apparently this is good for a 2.25 petrol ?
- Kenlowe only
working intermittantly. Faulty relay connections. Loose
wiring causing arcing and excessive heat. Stripped and
replaced connectors.Working fine now but will have to
consider locating all under bonnet relays in a sealed
box.
- Cartman
PASSED!! As I thought the emissions were high at 7% CO
(garage tweaked the mix to 4.5%), and the headlights were
low (they reset them). And for these two adjustments they
only charged me £3 over the MOT cost. Good work
fellas!!!!!!. I had an advisory though on one rear brake
cylinder that was 'sticky' (not returning quickly) and a
'squidgey' rear brake flexible hose. Ordered them from Paddocks and hope to get
them done in the next week. The mixture adjustment has
made him run smoother and quieter as well.
- The rear
folding seats never get used and are taking up load
space. They are not the most comfortable way for people
to sit anyway. I have a plan to sell all four of these
off and replace them with two forward facing folders from
BLRS. They are in reasonable condition and are preferable
to the 'standard' bench seat so hopefully I can sell the
whole set for around £70 which will at least pay for one
new seat? Two removed for now and if they are wanted I
can unscrew the other two in 15 minutes.
- Cartman is
due for another MOT. Booked in for Saturday 12th August.
General check over before the test. All lights
work,steering rigid and no excessive play; brakes are all
new and are almost bedded in now. Only points of concern
are emissions (passed last time OK-but played with it
since); headlight alignment (set it up in the car park)
and the frequency of the indicators (depending on their
mood anything from .1 to 1 second intervals).
- Tightened all
the suspension mounts and lubricated all suspension
pivots and springs - amazing,isn't squeaking now!
- New CB
antenna arrived. Had to mount this to the rear on the
gutter mount above the door. Matching on the side gutter
would not acheive an SWR better than 2 to 2.5. The rear
gutter sees 1.1 across the range of 27.951 to 27.551MHz.
Now suffering from loud 'twanging' as I travel down the
local lanes - surprising that!! Antenna kept inside most
of the time anyway.
- HBRO Bowhill
rally and driving day on the South Downs near Chichester.
Second gear on the box now starting to pop out on
inclines - not good. Need to check out the detent
springs.
Bowhill
Farm near Chichester 6 August 2000
- CB fully
fitted into Cartman with a gutter mount over the
passenger door. First outing and the antenna is sheared
off at the loading coil - as I left the drive. Need a
re-think on that one.
- Dismantled
the rear passenger hub. Oil seal and felt seal replaced,
bearings OK. Half shaft has signs of spline wear at the
hub end and past corrosion that has eaten away at the
thread. I'll look for another one and a castle nut at
Sodbury.
July
2000 (70500 miles)
- Found the
problem with the front brakes. The manual adjusters on
the front brake shoes would not permit full contact with
the drum (11" LWB hubs). Therefore, the initial
depression was forcing it onto the drum but allowed the
shoe to return back too far unless the pedal was
depressed soon after. Stripped down both front hubs.
Replaced the manual adjusters on both sides, as they were
worn, and also fitted new shoes as there were signs of
past contamination of the linings. Managed to pop out one
piston during assembly and had to bleed the whole system
through again.
- The front
passenger hub was also removed just as a preventative
measure and checked for bearing condition and the state
of both the oil seal and shaft felt seal. The bearings
were fine and were lightly re-packed. The oil seal was
replaced along with the felt seal. Freewheeling hubs
regreased with LM.
- Rear drivers
side hub was removed and the oil seal replaced. Though
the seal appeared to be in good condition the bearing/hub
securing nuts (52mm) were both loose and required only
hand effort on the hub spanner to remove them (after
knocking back the retaining washer). A new oil seal was
fitted. The bearings were in good condition though, but
required repacking with LM grease.I will also check the
other rear hub assy. this weekend. I will keep an eye on
this hub but I have to assume that the cause of the leak
was the excessive movement allowed on the seal which them
permitted oil seepage.
- Brakes are
still not what they were. Initial depression gets them
working but a second depression within 5 seconds improves
them no end. Most people that I refer this problem to say
the usual leaking pistons. But they are fine. It seems as
if the pistons move the shoes out and then they slowly
retract under spring pressure against the hydraulic
action of the pistons. Maybe the master cylinder? I need
to dismantle and check them again.
- Rear drivers
side hub is now leaking EP90 very slightly. The passenger
side failed and was replaced just over a year ago so its
about time this one went as well. This time I want to
rectify the problem myself. So a delve into the Haynes
manual is called for. I picked up a hub spanner at
Sodbury so it may now be put to good use.
- Wheels &
Tracks at Bordon sources another gear knob (Nice shiney
and new, and I can excuse the extravagance as it was only
a £1) and a new reversing light. The old lamp was
getting yellow and brittle.
June
2000 (70200 miles)
- Fan belt
squealing. Adjusted.
- Tappets
adjusted, plugs cleaned and points re-gaped. Whoops,
rocker gasket that I picked up at Sodbury is the wrong
type, pooh. Luckily the local auto factors can get one in
next day. More mud found in the radiator cooling fins
(from scenic drive at the ARC). Brushed and washed out.
Seems that the engine is running cooler now. Surprising
that?
- When I
purchased Cartman he was equipped with one of those
in-line fuel devices intended to allow you to run the
leaded head on unleaded. Every publication that I have
ever read has said (other than the manufacturers
suppliers bunph) that they are unproven. So off it came
and still resides in the corner of the garage. Since then
I have been running with either Castrol standard lead
replcement additive or the octane booster equivalent
(this does work well). Now this head has been subjected
to lead or 'equivalent' lubrication and anti-knock
additives for 22 years so how long would it carry on
working before it required hardened exhaust valve seats I
wonder? Additive works out as an additional cost of 2-4p
per litre and with the cost of petrol creeping up (yet
again) I am considering just running unleaded. Several
people I spoke to at the ARC are doing just that with one
individual acheiving 15k miles with no noticable ill
affects.
Or, I just
bolt the in-line unit back in and stop putting in additive.
This cannot be worse than using none! Watch this space and
see how we get on.
- Rear brake
shoes replaced with Mintex equivalents. I have heard so
many horror stories about bleeding the braking system on
series vehicles and dreaded carrying this out so the ease
at which it was achieved (on my own) came as an
anti-climax.
Some years ago
I purchased one of those Gunson's 'Easy bleed kits' that
attach to your master cylinder reservoir and pressurize the
brake system with the tyre pressure. The only problem I had
with this was that the joints on the rubber connecting pipe
between the reservoir and the master cylinder were not sealed
for pressure and would then weep. A couple of tie wraps at
either end stopped this. I bled the whole system through and
replaced it with new DOT4 fluid in about 1 hour including
removing all four 750's.
- Using the
Halfords two part flushing agent I spent around 2 hours
flushing through the whole cooling system. I believe a
lot of crud found its way out but I cannot be certain.
But the running temp of the engine is still sitting at
just below the red even with the Kenlowe at full chat.
Could it be that the temperature sender has developed a
fault? That is now the only item left in the chain. But
the engine definitely warms-up quicker now.
- Water
pump,'stat',rad top & bottom hose etc. were fitted
but the engine was still heating up past half way. My
theory is that the original over-heating from the ARC has
caused a lot of rusty sediment to become dislodged and
block up some of the rad waterways. So the next item will
be to flush out the whole cooling system.
May 2000
- Back from the
ARC and 3 days of Scenic Drive marshalling have left
their toll. Brakes are now spongey, hand brake almost
useless, water pump leaking and horn now sounds like a
tortured rodent.
- Hand
brake assy dismantled and adjusted - OK
- Horn
(removed liquid mud) and added a second, both now
relocated away and up from the front grill.
- Main
brake drums dismantled,cleaned and adjusted. Back
shoes were worn past caring on the trailing edge so
they require replacement.
- Water
pump leak caused us to stop 3 times on the way back
from the ARC to top-up then mysteriously rectified
itself. Not to be relied upon so I have a new pump,
'stat and rad cap to fit this weekend.
- Both
diffs,tx box,gbx,o/d and engine were all drained and
oils replaced (no evidence of water), the right-hand
front hub had some water in it but the left was OK.
Both were refilled but I will keep an eye on the RH
one.

- Drivers
door barrel fitted. 'Wayhay' we now have a 'secure'
vehicle. Modifying the passenger door to accept a key
lock will have to wait until after the ARC - too much
other stuff to do.
- Rear
door barrel fitted so only two to go now. Managed to
shuffle my wifes motorcycle from across the front of
Cartman and extricate him (despite the lack of a front
wheel). First laning trip for 3 weeks - nearly got
stuck!! Newly painted door gets scratched.
- One
week later one door lock turned up. Not 2 as ordered,
just 1. To top it all despite their incompetence at
supplying the wrong part they then charge my credit card
(without consent to the sum of £4 - not a lot but it is
the principle of the thing) Why do we deal with these
people? I'll remind myself next time not to deal with
Cra*****s.Given up with mail order for now. Visited
Kingsley Cross Country near Bordon and ordered them there
(they also give an HBRO discount).
- Ignition
lock and a pair of door lock barrels arrive. Ignition
lock is OK and goes straight on but the door barrels are
the wrong type. The supplier says, 'Send them back with a
sketch of the correct type and I will send the others by
return of post'.
April
2000
- While the LR
is 'off-road' due to lack of locks I decided to try my
hand at painting. Removed drivers side door, filled all
the dents, primered and rollered a new coat of enamel on.
Not a bad finish even with this method of application.
Pity about the flies that decided to exhale their last
breath on it though. Liz say's that there is little point
in painting it as it will only get scratched. I will need
to rub it back at some point though to remove some of the
runs at the top curve of the door - at some point.

- One bulb has
failed on the new 100 watt spots already. A Disco driving
colleague reported the same fault and has heard of
others. It seems that the lamp assembly cannot dissipate
the additional heat that this size of bulb generates, the
bulb eventually overheats and blows. I had a couple of 55
watt bulbs available and those were popped in. No
problems since.
March
2000
- Successfully
finished the installation of the two 100 watt Ring Phaser
halogen front spots and a set of rear axle check-straps.
Bit more Waxoyl on the exposed rear underside.
- Stripped down
rear door. Welded-up the cracked frame, replaced the
bottom strip (rusted) and welded in some re-inforcement.
1" thick sound-proofing fitted as well. 6mm thick
tread plate fitted to the interior of the door. This
re-inforces it tremendously. It's now rigid as a very
rigid thing.
January
2000
- Charge light
seems to be always on on the dash. It was definitely due
to the battery as the next day it did not want to start.
New battery was fitted. At the same time the alternator
output was checked and found to be 15.2 vdc. A bit high
and was not doing the battery much good (this is also the
source of the charge light indicator signal). This was
also replaced with an exchange item. No more problems
there.
- Cartman's
first off-road driving day with Hants & Berks results
in a bent wing and nearside sill. Closer inspection
reveals that the passenger floor pan was also damaged
beyond repair when the wing support bracket pushed up
through it.
I had a
footwell section spare so this was welded in. The wing was
pushed out with the aid of a scissor jack. The original
footwell was severely rusted anyway so I did it a favour. For
damage limitation I fitted some aluminium sill protectors and
rear corner unit - until next time. A few sections of
scaffolding pole are lying in the garden and may be fitted
later also.
- Numb bum
prevention. BLRS kindly supplied me with a pair of front
high back seats - in exchange for some cash.
Any comments
regarding manufacturers or suppliers parts or services are only
from my personal experience. Those items I find to be less than
satisfactory I will state that they are not up to scratch, and if
they're good then I will say so. I am not associated my marriage,
employ, or money (unfortunately) with any of those companies
mentioned.
Paul Maidment
- 11 June 2000



Updated
13 January 2003
me at
pjboomer@freeuk.com 