2002


This
page is intended as a historical/hysterical record of the the
past breakages/new breakages and soon to be breakages....and
other bits that have happened to Cartman (and fallen off) since
we first adopted him. This record is in the order of most recent
happenings at the top to the past at the bottom.
Work still on Cartman's
ongoing to do list....!!!!!  |
Fit
air intake snorkle.
Advance the distributor timing a tad. Currently 6 Deg.
TDC
Aquire
some spare rear half-shafts :)
Steering guard being slowly fabricated.
ETA 2005! :)
Waxoyl
the whole chassis after a steam clean.
|
December
2002
- Alternator
bearing is packing up. Obvious really when you hear the
loud rumbling :) Another ordered from Paddocks (£22) .
That's what happens we you keep imersing it in muddy
water.
- Modded the
rear panels behind the rear wheels with the grinder to
allow the mud to fall out easier and more efficient jet
washing. Originally I had considered doing this but
decided against it so as to 'not ruin the original looks
of the LR'. But stuff it, it needs to be used so mod as
nec. :)
- Weird wiring
problem saw the failiure of all the headlights and
sidelights after some energetic jet washing over Xmas.
The unusual fault turned out to be a corroded +12vdc
connection at the battery which acted as a high
resistance point under load. So without load there was
+12v to the lights and when under load it dropped away to
zero. Most confusing. Rewired and increased the cable
CSA. Then coated with vaseline - so hopefully that won't
happen again.
- Engine oil
flush and oil change. It is only about 2k miles (if that)
when I last swapped it but a persistant leak from the oil
filter needed resolving and this would kill two birds
with one stone, as it were? The oil was clean before I
dumped it but after 15 minutes with STP engine flush
resulted in a black oily mess deposited in the collection
bin. Refilled with halfords 'standard' 10/40 this time.
Filter leak was due to me poorly fitting the last filter.
- Re-grease all
prop UJ's and check OD/gbx/tx/diff box oil levels.
November
2002
- Nothing much
happened this month :)
October
2002
- Sodbury on
the 26th yielded the 90 door wheel mount for £10 I was
after and a new set of Raydot spots. Fitted the spots and
tyre mount over the weekend. As the tyre is now mounted
slightly further out than before I took the oppertunity
to fit the third hinge that I had had for a while and
then to weld up some cracks found in the re-inforced door
frame. Due to poor 'slug scattering' in the past. It
might not be pretty now, but it is strong.
- Managed to
find some time to check and top up all the transmission
oils and hubs after the dunking incident. The only sign
of water ingress was around both hubs which were
completely drained and refilled with EP90. Also pumped
all prop UJ's and sliding spline with fresh LM grease
until clear.
- Washed the LR
down three times starting with the hose and then the
pressure washer to thoroughly clean the chassis inside
and out etc. Ideally I need the chassis steam cleaned and
then give it another Waxoyl and Dinitrol inside. It had
been 2/3 years since this was last done.
September
2002
- Now the No.1 rule of green
laning is never to go out alone,
and have the necessary recovery equipment. So what do I
do? Pop out for a few minutes straight onto the Plain and
the lure of mud then takes hold (the brown mist?). Find a
muddy hole and drive through a few times, which was nice.
Then decide to go in a bit further and a bit faster and
'slikkkk' I'm stuck. No one visible for miles and Carty
is stuck past the diffs with muddy water lapping against
the bottom of the passenger window (I'm pleased I sorted
those door seals out now). Luckily I managed to extract
him after 20 minutes of working the groove/rut down to
firmer soil/mud with the aid of the Guyanes. And reversed
out of the hole. If it wasn't for the Guyanes I would be
there now. So I have learned that though you may have
nover been stuck before -- IT WILL HAPPEN eventually so
take precautions! Carty now needs a thorough going over
as the exhaust has taken on quite a different tone (mud
in the baffles?) and the handbrake don't work too well :)

- Fitted the
new speedo cable and it was bad enough trying to route it
over the gearbox but then the three 'silly little' screws
that secure it to the speed drive assy on the gearbox
were a complete bunghole. Either the transmission barke
ot the overdrive seemed to be in the way, but I managed
it in the end - lost one screw though. Topped up the
gearbox and transfer case while I was at it and added
some Wynns gearbox stop leak in the main box. Maybe that
will reduce the EP90 deposits ?
August
2002
- Picked up
carty with the replaced short drivers side rear
half-shaft replaced. The original one had failed at the
differential end. At the same time Mark had spotted that
the oil seal on the diff output to the prop was leaking
and replaced that as well. I knew it was weeping and it
saves me doing it. Then on the way home the speedo cable
bust. Turned back to West 4x4 and picked up another to
fit later. Price £6.50.
- A bit after
it started running rough I had stopped off at a recent
neighbour to pick up some mail and reported to them it
was running rough but I would make it back all right. 100
yards down the road I pulled gently away from an
inter-section and a rear half-shaft snapped. After a slow
realisation of the problem the free-wheeling hubs were
re-engaged and I put it in 4WD and drove it 6 miles to
West 4x4 in Swanmore for the fix. I could have made it
the 40 miles back with the front wheels fixed but I
didn't want to risk possible damage and I don't have the
time after the house move to fix it at the moment.
- After the
house move to Wiltshire I had to return the trailer to
one of its rightful owners back in Hampshire so I started
the South bound slog one Saturday morning. The sun was up
and the engine was getting warm (but the newly adjusted
Kenlowe and coolant system was running fine). Once I had
done around 40 miles it started idling badly. It was now
lumpy but ran fine once I started accelerating. No
pinking was noticed but the engine was running hot. Once
the engine had been left for an hour it ran fine on
tickover. It sounds like it has been too far retarded.
I'll adjust it back 3-4 Deg. to start with and see how we
go (3
Deg. TDC recommended by R.Turner on LRE Forum for 95
Octane fuel).
- Though the
ignition seemed to be set close to what it should be
after setting it by ear (just
starting to pink on heavy load) I
thought I would get it set 'professionally' just in case.
We were moving house in a couple of days and as we were
pulling a 1 tonne trailer it would be wise to give it a
check over. The mobile tuning guy (Shire club member)
reported that the timing was 24 Deg. too far advanced!!!!
So why was it only just pinking? Reason unknown. So he
set it to 6 Deg. before TDC as the book recommends. It
seem to recall several comments on the LRE forum
regarding the inaccuracies of the crank timing marks
anyway. The CO was also around 8% and after adjustment it
was down to 3.5% at tickover. The first run after
adjustment revealed that we now had better 'bottom end'
pulling power but downhill it was popping badly and had
started overrunning badly, just as it used to. Too far
retarded?
July
2002
- Major oil
leak from the transfer box was narrowed down to an access
plate on the transfer box that I had not fixed a gasket
to. I had only used blue Hylomar. The sealant had
eventually dissolved allowing oil to get by under
pressure. Fitted a card gasket coated with 'blue' and
refitted. Transmission still leaks but it is only around
30% of the original leak :)
- Fitted the
Pertronix ignition and the Lucas gold coil. Starts easier
and runs a tad smoother. Old points and condenser are
held in the cubby fo safe keeping :) Timing set to TDC as
recommended by Aldon/Pertronix and then retarded slightly
to avoid 'pinking' under load. Bosch 4 probe plugs
cleaned and each electrode gap opened up to 0.9-1.0mm
using a paper clip as a go/no-go gauge. The
Aldon/Pertronix Ignitor for the Lucas 45D4 distributor
costs £70 delivered in the UK and can also be sourced in
the US as either an LU143 or 144 at $70 (around £50 in
UK money!).

Before,
after and after the mod was installed
- For a cheap
method of fitting electronic ignition to a 45D4
distributor click here. £5-£10 and a
few hours labour will save you around £40.
- To circumvent
the points (and prob condenser) prob I will install an
electronic ignition module inside the existing
distributor (Aldon/Pertronix Ignitor) along with a 42kV
Lucas gold coil (Aldon/Pertronix
FlameThrower coil is the same spec but costs £22 more!).
The other benefit being a larger spark (plugs opened up
by an additional 5 thou. over std 32 thou. gap) and
improved 'timing' of the ignition spark. Ordered 16/7/02.
- So I decided
to carry out a few changes and fit the MSD Blaster 2 coil
and open up the points by 5 thou. Initially it ran well
(on the drive) but after trying to move towards the road
it started to miss and then ran on 2 cylinders. After a
lot of searching the fault was the points which showed
evidence of excessive surface arcing and were sparking
when the engine was wound over. Managed to get the engine
running after opening up the points and replacing the
coil with the original std one. After investigation the
MSD Blaster primary was found to be only 0.7 Ohms and the
original was around 5 Ohms - so all lot of extra current
for the std points to cope with? Both the points and
condenser died though, the condenser was probably on its
way out that is why we were having all of the problems?
- After the
Beaulieu 4x4 Show the engine started to 'pink'/pop on
down hill sections and generally have a lack of power.
All last week it had been running brilliantly. Checked
the distributor for movement and the points - both were
fine and no evidence of change there. Once it had cooled
down though it seemed to run better. So next I stripped
the carb and checked for anything that could be causing a
weak mixture there - no problems found.
- The two
aluminium mud shields I bought at the last Sodbury
Sortout had to be fitted at some point so I decided to
get at least one completed as the sun was out and I hoped
it would not take too long. Luckily it didn't and the
passenger side one was off and a new one in in around 1
hour. Coated it with black underbody gum to deaden the
sound of flying mud.
- Carty had
developed a rather course pop on overrun. Also if you hit
a puddle a speed the ignition system will baulk where it
had never baulked before. He wades 2ft. without a prob,
or at least he did. Returned home from a short run on
evening with the engine nice and warm to regap the valves
(20 mins. all in there) and thought I would take a look
at the distibutor. Took off the mud shield I had placed
around the dist and looked at the cap - what do I see but
a hairline crack from the base of the cap to the top.
Luckily I had, on that day,purchased from Bearmach in
Maidstone a new cap, points, condenser and rotor arm -
pure coincidence? Fitted the lot and it purrs now (after
I remembered to fit the rotor arm back in-Duuhh! ).
No popping on overrun and no run-on (yet, but I have said
that before); ticks over much smoother as it was erratic
before; and is not suffering from moisture probs. Superb
!!!!
- The ongoing
tweaks and fiddles with the carb have resulted in the
first mpg figures for the consumption page. After two tank
fills with the 170 main jet in the Weber on 205's have
revealed a fuel drinking rate of 19.2mpg. This was after
the full carb strip-and-rebuild that had not originally
envisaged after starting the main jet investigations. The
main has now been increased to a 175 (the original US
suggestion) and we will try another couple of tank fulls
to see how this performs.
June
2002 (78100 1/7/02)
- We have now
got to the point where I have to get the Speedi-Sleeve
fitted to the transfer box rear output shaft to reduce
the leaks. Bought the (CR99162 BSL ref.) sleeve repair
device from Blue Diamond for £18+vat (BSL do it for
£16.50+vat) but are a 15 mile round trip. Drained the
transfer box and dropped the rear shaft and removed the
transmission brake drum and output shaft assembly
together. See fig.# for the scoring on the shaft. Removed
the shaft seal and refitted a new one (took two attempts
as I completely butchered the first) with blue hylomar
sealant around the edge to take up any scoring around the
transfer box face. NOTE:- When fitting the seal use the
round end of a hub nut box spanner as it fits nicely when
pushing the seal home. The Speedi Sleeve went on over the
shaft and then re-assembled with 2.5 litres of fresh EP90
GL4. Guess what..................there is still as much
of an oil leak as before (or such a reduction as makes no
odds:) It appears that the leaks are coming from higher
up the tx box and gbx. Selector rods again? BU***R!! Just have to keep
topping it up then ?

- Modified the
gearbox/overdrive/tx box and back axle breather runs so
that they now go into a communal manifold under the
centre seat box and then vent into the rear cab area.
This reduces the pipe run which was leading to blockages
and allows the line to be blown clear with far more ease.
- Replaced the
jamming choke cable with a new one from the local
motorists discount centre Les Smiths of Eastleigh at
£3.99. Blow the expense (original
Weber version £19 from Paddocks).
At the same time the Weber choke flap return spiral
spring had insufficient tension to close the flap fully
once the choke was pushed in. So the carb was removed
again and the spring tension increased by one additional
turn. Works a treat now. I now need to run the S3 for a
couple of tanks of fuel to determine how much improvement
there is with the rebuilt carb while running on the
205's. Once this has been determined I will switch back
to 7.50 AT's for comparision then the mud spec. Guyanes.
- Engine has
now started to run on again after a fast hot run. So the
problem was not just the carb. If I leave the engine
ticking over for a while after stopping the run-on does
not happen so it may be due to exhaust leaks still - even
though the manifold is not showing signs of leakage.
May
2002 (77728 21/5/02)
- Seems to be
running very rich after the LRE ramble and runs rough.
This happened while on The Plain and intermittantly had
trouble ticking over. I initially thought that it was due
to dust blockage of the K&N and the new 175 main jet,
but it turned out that it was not. The K&N was
thoroughly cleaned and re-oiled and it ran well at first,
but the then problems started again. So carb out and
stripped. The first item found was the air intake tract
was blocked with a piece of silicone from around the edge
of the K&N which was limiting the air intake - so it
allowed the engine to run rich when the piece was jammed.
So all were jets removed and the body and jets cleaned
with carb cleaner. Left the 170 jet in for the moment
(may go back up to the 175) and re-assembled with new
gaskets. The carb is now back on and its going well (even
have the rear wheels squealing off the lights now but
better stop doing that or it will be goodbye half shafts)
. I have no-longer had any problems with run-on for some
weeks now so all this re-jetting and carb mods must be
doing something right?
- Fitted a
'new' rad (£10 from Dave) and flushed the cooling system
through. Refilled with 40% anti-freeze. The old rad was
30% blocked with mud and was falling apart (crumbling) on
the cooling vains so a swap was a good move. Running
cooler now at around half way up the temp. gauge.
- LRE ramble
saw both spots 'disappear' somewhere on 'The Plain' after
a rather deep pot hole on the byway. So I need a couple
of those- pooh.

- Jets changed
on the Weber. Currently a 165 main jet as supplied with
the carb as std but as it is now fitted with a K&N
and the additional breathing that this provides it was
felt that an increase in size was required. So both a 170
and a 175 size jet were sourced from BHB Engineering in
Southampton and we then fitted the 175.

- A spare flexi
Friday saw a lot of odd jobs sorted on Carty:-
Front
shock rubber replaced; Overdrive drained and filled with
Semi Sythetic gear lube; Cubby box fitted with stereo and
cigar lighter socket for the cool box; Hubs/gearbox/tx
box/diff oil levels checked and topped up; Prop UJ's
checked and re-greased . All ready for the LRE forum
Salisbury plain ramble.
- Cartman is
running very well at the moment but hopefully he will be
running even better soon. After the last trip to the USA
and meeting up with another bunch of LR enthusiasts in
the CT./RI. area I have now found out what main jet to
fit to the existing Weber 34ICH carb to compensate for
the fittment of the K&N filter. Apparently the std
fittment is a 165 jet and it was upped to a 175 (.0165
and .0175?). I have ordered said jet and hope to get it
fitted this month and give it a go so watch this space
for an update.
- I was also
given two 'one piece' door seals from a '97 90 and set
about fitting the to the S3.
1. Remove
the original seals by drilling out the rivets retaining
the original seal strips and chuk 'em.
2.
Grind/cut the outer lip around the door seal mounting
strip (galv and ally) down to about 2mm.
3. Place
masking tape behind each rivet hole and seal the holes
with quality silicone (high temp solvent type prefered).
4. Seal
the groove between the windscreen top and door frame etc.
5. Coat
the edges of the door seal mounting with quality silicone
RTV/sealant.
6. Tap the
new seal into place (raw hide mallet) and trim the new
seal at the latch point and windscreen hinge with
aircraft snips or similar.
7. Leave
the silicone to set.
8. Remove
the masking tape.
9. C'est
finit :)
It is now
quieter inside and doesn't leak - as much :)
- Aquired an
original LR cubby box in mint condition for the S3. It's
grey and doesn't match the black seats but one cannot be
too fussy can one :) After 2 years I have acheived at
least one of my goals and got that item fitted.
April
2002
- Front
Bearmach sidelamps had finally corroded to such I point
that I have given up with them and have ripped them out.
Ordered a replacement set from Paddocks - and the ones
that arrived were also Bearmach. The new ones were of a
different design though with a condensation drain and
less 'corroding' metal. Fitted new lamps and improved the
cable seals with self-amalgamating tape and silicone.
- Crack found
in the front drivers side (RH) dumb iron just behind the
front spring hanger. This had been 'repaired' by a
previous owner and was now very corroded on the underside
and had eaten through. So a morning of other planned jobs
resulted in cutting out the corroded material and
re-plating the section of 2mm steel plate.
- Carty is
still running better after the vac advance pipework
change but the running on and popping on hill decents has
returned.
- Replaced the
front section of the exhaust to discover that the
evidence I had seen around the manifold/downpipe joint of
leakage was not due to a damaged exhaust section but a
previously brazed in stud that had pulled through
(therefore working loose with expansion contraction). The
new exhaust section was only £12 so this was fitted
along with an 6mm SS bolt as a temporary replacement. I
am planning to fit a new manifold gasket anyway so when
that is off I will thread the exhaust manifold to 8mm and
fit an SS studs and lock nuts.
- Transfer box
breather found to be blocked after a green lane day
around Salisbury. That's why it was pressurizing - again.
Could not find the blockage so the only option was to run
a new pipe section through.
March
2002
- The result of
replacing the advance pipework and dumping the 'black
blob' has resulted in a transformation of Cartman into 'Sports
Cartman' Only kidding.
Smoother/quicker/quieter, plus its now running on road
going 205's. No running-on/no popping on foot off hill
decents (see above!).
I suspect that this was fitted by a previous owner along
with the 'Catalyser' unit that was bolted in the fuel
line to 'allow you to run the vehicle on unleaded without
additives etc.' - not that I do. I use Castrol additive
on unleaded. They were probably under the misguided idea
that this would work.
- Polyurethane
pipe fitted to replace the vac advance pipework and I
also removed the small black one way/damping valve to the
distributor which was fitted in-line with the pipe. The
unit was marked 'Ford' (Eeeh) 'Distrib' on one end and
'Carb' on the other. No-one on the LRE Forum could give
me a suggestion as to it use or even whether it should be
even fitted. Seems to run fine with it removed but I will
give it a few days to check it.I could find no reference
to the valve in either Haynes or the 'Green bible'
either.
- Aquired a set
of 5 new Mangles grey modular rims. Four of these came
with 205's fitted. Not a lot of tread left but legal. So
for a change I fitted these instead of the 7.50's to see
what difference these make to the 'performance' and
gearing. Initially the acceleration is much better (it
would be with smaller dia. wheels-duuh) and the gears are
used a lot more. I have had the larger 7.50's on almost
since we bought Cartman and I was going to lob the 205's
and fit the spare 7.50 AT's but its an interesting
comparison none the less. Now I expected a gearing
difference for their 3-4" reduction in diameter but
the transformation along with the vac pipe replacement is
amazing. It may well be the pipe change (above) as well
but I can now accelerate and the reduction in tyre
sidewall height has made bends and roundabouts much less
of a wobbly 'manouver' :)

205's
V 7.50 Guyane's
February
2002
- Following on
from the carb adjustment thread the exhaust is now
'popping' on downhill road inclines with my foot off the
throttle, but run-on is almost non-existent. So it must
be close to the mark? It still seems to be lacking at the
top end though. So I am going to replace the distributor
vac advance pipe from the inlet manifold. It still has
the original copper tube type fitted with loose 'rubber'
ends. I'll replace this with 6mm OD Polyurethane.
- Brickiln Farm
Challenge on the 24th. A few pics from a very wet and
muddy day.
- The
windscreen wipers are now 18 months old and the blade
rubbers stripped on the drivers side (luckily, when there
was no rain:). Replaced with rubber wiper blade sections
from Halfords for £4.50.
- After the
probs below I decided to reset-up the Weber following
advice logged on the LRE forum. Wound the carb mixture
jet carefully in until it bottomed out. then wound it
back two full turns. Started the engine and set the
tick-over for as slow as possible. Adjusted the mixture
until it ran as smoothly as I could get it then reduced
the tick-over and repeat. Once I was happy with this I
adjusted the idle back to around 800 RPM (no tacho) and
took it for a run. I no longer have the run-on problem
that I previously had and the engine is running cooler
but its pinking under high load. Richened up the mixture
by 1/4 turn and it no-longer seems to pink but it ran on
this morning (a little though). I'll try it for a few
more days and see how it goes.
- Not running
very well after I noticed that the K&N was not
fitting tightly to the Weber and replaed it with the
original oil bath filter for a day. The oil bath unit had
been lying on the floor of the garage for around 2 years
and had collected its fair share of insects. So not
cleaning it out first the first 20 miles had it running
very erratically at tick-over. One can of carb cleaner;
some Wynns fuel system cleaner in the tank with a new
tank of fuel and the K&N refitted (plus new Champion
plugs) saw the problem go away after 60-70 miles. Dirt (spidey
legs) must have become stuck in the
idle jet?

The
old Valeo plugs after removal - mixture looks about right?
- Shire LRC
green lane day on the 10th saw Dave's hybrid throwing a
wobbly after a 45 Deg. climb. It did not want to fire at
all and had to be towed half way home - then it decided
it had had a rest and ran.

January
2002 (76500miles)
Any comments
regarding manufacturers or suppliers parts or services are only
from my personal experience. Those items I find to be less than
satisfactory I will state that they are not up to scratch, and if
they're good then I will say so. I am not associated my marriage,
employ, or money (unfortunately) with any of those companies
mentioned.
Paul Maidment
- 11 June 2000



Updated
13 January 2003
me at pjboomer@freeuk.com 